CR27/Cleburne Co. over BIG CREEK
Facts
Source: National Bridge Inventory. Information not verified; use at your own risk.
Name: | CR27/Cleburne Co. over BIG CREEK |
Structure number: | 000000000020058 |
Location: | 1.25 N W JCT CO 35 |
Purpose: | Carries highway over waterway |
Route classification: | Major Collector (Rural) [07] |
Length of largest span: | 16.1 ft. [4.9 m] |
Total length: | 32.2 ft. [9.8 m] |
Roadway width between curbs: | 10.8 ft. [3.3 m] |
Deck width edge-to-edge: | 12.1 ft. [3.7 m] |
Owner: | County Highway Agency [02] |
Year built: | 1965 |
Historic significance: | Historical significance is not determinable at this time [4] |
Number of main spans: | 2 |
Main spans material: | Steel [3] |
Main spans design: | Stringer/Multi-beam or girder [02] |
Deck type: | Concrete Cast-in-Place [1] |
Wearing surface: | Monolithic Concrete (concurrently placed with structural deck) [1] |
Latest Available Inspection: July 2018
Good/Fair/Poor Condition: | Fair |
Status: | Open, no restriction [A] |
Average daily traffic: | 55 [as of 1987] |
Truck traffic: | 1% of total traffic |
Deck condition: | Satisfactory [6 out of 9] |
Superstructure condition: | Good [7 out of 9] |
Substructure condition: | Good [7 out of 9] |
Structural appraisal: | Somewhat better than minimum adequacy to tolerate being left in place as is [5] |
Deck geometry appraisal: | Basically intolerable requiring high priority of replacement [2] |
Water adequacy appraisal: | Basically intolerable requiring high priority of corrrective action [3] |
Roadway alignment appraisal: | Basically intolerable requiring high priority of corrrective action [3] |
Channel protection: | Bank protection is in need of minor repairs. River control devices and embankment protection have a little minor damage. Banks and/or channel have minor amounts of drift. [7] |
Pier/abutment protection: | Navigation protection not required [1] |
Scour condition: | Bridge foundations determined to be stable for assessed or calculated scour condition. [5] |
Sufficiency rating: | 51.4 |
Recommended work: | Replacement of bridge or other structure because of substandard load carrying capacity or substantial bridge roadway geometry. [31] |
Estimated cost of work: | $216,000 |
Previous Inspections
Date | Condition | Deck | Superstructure | Substructure | ADT | Suff. Rating |
---|
July 2018 | Fair | Satisfactory | Good | Good | 55 | 51.4 |
July 2016 | Fair | Satisfactory | Good | Good | 55 | 51.4 |
July 2014 | Fair | Satisfactory | Good | Good | 55 | 51.4 |
July 2012 | Fair | Satisfactory | Good | Good | 55 | 51.4 |
August 2010 | Fair | Satisfactory | Good | Good | 55 | 51.4 |
December 2009 | Fair | Satisfactory | Good | Satisfactory | 55 | 16.1 |
November 2007 | Fair | Satisfactory | Good | Satisfactory | 55 | 49.7 |
October 2005 | Fair | Satisfactory | Good | Satisfactory | 55 | 49.7 |
October 2003 | Fair | Satisfactory | Good | Satisfactory | 55 | 49.5 |
October 2001 | Fair | Satisfactory | Good | Satisfactory | 55 | 49.5 |
October 1999 | Fair | Satisfactory | Good | Satisfactory | 55 | 49.5 |
October 1997 | Fair | Satisfactory | Good | Satisfactory | 55 | 49.5 |
October 1995 | Fair | Satisfactory | Good | Satisfactory | 55 | 49.5 |
November 1994 | Fair | Satisfactory | Good | Satisfactory | 55 | 49.5 |
November 1992 | Fair | Satisfactory | Good | Satisfactory | 55 | 56.5 |
December 1990 | Fair | Good | Good | Satisfactory | 55 | 56.5 |